Spidery (manifold) goodness -> issues++
Spidery (manifold) goodness -> issues++
Good to be back!
Been stuffing around troubleshooting these problems, and would value any opinions/suggestions from anyone who has been this dark path of sorrow previously...
have an EA82T L-seies conversion from an australian delivered donor car
Fitted a spider manifold with an RS IC and experienced issues since - mainly idle and fuel eccomony, BUT it goes much harder.
Issue 1: idle is rough & high despite modifications to TPS, hot/cold running etc. ECU consistantly shows no fault codes.
Issue 2: Ecomony - about 275km tank driving nice. Going hard about 250km with black gunge over the tailgate. This was an issue B4 the manifold was fitted, but not as bad. Std boost
Had injectors cleaned - very very gummed up (despite only using PULP). since cleaning car runs better, more power, but ecomony is unchanged.
Swapped both the AFM, dizzy & ECU with a RX that returns 12ish lt/100 - no difference !!
Sooo, given there has been much stuffing around trying to get this right, (thanks muchly to Steve B) was thinking a WOLF 3D would be way to go - any suggestions / tips / comments heading down this path?? Anything I've missed??
thanks[/u]
Been stuffing around troubleshooting these problems, and would value any opinions/suggestions from anyone who has been this dark path of sorrow previously...
have an EA82T L-seies conversion from an australian delivered donor car
Fitted a spider manifold with an RS IC and experienced issues since - mainly idle and fuel eccomony, BUT it goes much harder.
Issue 1: idle is rough & high despite modifications to TPS, hot/cold running etc. ECU consistantly shows no fault codes.
Issue 2: Ecomony - about 275km tank driving nice. Going hard about 250km with black gunge over the tailgate. This was an issue B4 the manifold was fitted, but not as bad. Std boost
Had injectors cleaned - very very gummed up (despite only using PULP). since cleaning car runs better, more power, but ecomony is unchanged.
Swapped both the AFM, dizzy & ECU with a RX that returns 12ish lt/100 - no difference !!
Sooo, given there has been much stuffing around trying to get this right, (thanks muchly to Steve B) was thinking a WOLF 3D would be way to go - any suggestions / tips / comments heading down this path?? Anything I've missed??
thanks[/u]
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thanks guys
O2 sensor: new unit
H2O sensor: also swapped, works fine, no codes
Mixture: nope, tailpipe CO readings spot on, EXCEPT coming off cruise, soooo,
Current thinking it's the valve hanging off the dizzy that contributes to ecconomy - ordered a new one & will fit next week.
Geach, drop the turbo by anytime - am headed out to Rising Sun (probably) Wed/Thurs this week. And was your white RS wagon (lowered now?) TR into Henely Beach off south in a powerslide about a week or two ago??
O2 sensor: new unit
H2O sensor: also swapped, works fine, no codes
Mixture: nope, tailpipe CO readings spot on, EXCEPT coming off cruise, soooo,
Current thinking it's the valve hanging off the dizzy that contributes to ecconomy - ordered a new one & will fit next week.
Geach, drop the turbo by anytime - am headed out to Rising Sun (probably) Wed/Thurs this week. And was your white RS wagon (lowered now?) TR into Henely Beach off south in a powerslide about a week or two ago??
LOL!Stevie-L4EVA wrote: Geach, drop the turbo by anytime - am headed out to Rising Sun (probably) Wed/Thurs this week. And was your white RS wagon (lowered now?) TR into Henely Beach off south in a powerslide about a week or two ago??
nope not me! i like my licence where it is - in my wallet. were the plates RST 555? i'm RST 092
PM me your address and i'll drop by sometime soon. i'll ring steve and let him know its on the way.
have you got at least one of the vacuum switchs on the the right hand strut tower hooked up? i disconnected the boost/fuel cut and left the line for the boost light in place because the ECU requires a signal. i beieve that computer and motor is an 85/86 model with the 4(?) plug ECU.
it had behaved as you describe with them both unplugged.
it had behaved as you describe with them both unplugged.