Today was more sweet than bitter but it could have easily turned horrible.
Took off at 6:30am bound for Croydon to my friends at VW performance Centre. Got to yea and broke down at the servo when Tweety's engine wouldn't restart.
Turned out much later that there was a lot of condensation in the electronic dizzy. Not the first time!
Eventually restarted and the engine broke a supercharger belt at Glenburn. Inspection revealed the belt had a tendency to move towards the engine. Later Daniel from VWPC found it was out iof alignment by about 3mm resulting in one of the 5 ribs on the belt to fray, break then the rest of the belt followed.
Luckily I had a spare and pushed on from Yea to Ringwood East where the second belt snapped. I heard it go. But pushed on regardless and found that indeed the engine can maintain power without the belt...no boost of course.
So Daniel took about 2 hours to make a spacer between the crank pulley and the SC ribbed pulley, plug weld it together etc. Then it was dyno time.
I had had 145's as a main jets in the 40 DHLA Dellorto,. In the end we had 225's so you can imagine how lean it was running. Air jets were matched. Accelerator "pump" jets had to go to greater sizes too. Initial runs were disappointing. Last years HP maximum was 60 hp at the wheels. These runs were 58. I asked Daniel to check the throttle. Yep...less that half effective throttle when squeezed tight- my fault. We spent some time remaking a better throttle set up with more throw and a better link.
82.2 hp at the wheels compared to 59.6 last year. a good jump of 32% in hp. I began to raise a smile.
Torque last year was 440lb this year 570. another substantial increase.
Here is the graph. The green is last years results after the weber carb was installed. Todays is in red. Power is the humped curve, torque the flatter lines.
That was at the wheels. last year the flywheel HP was 75. This year....well we got it way up toward 98 then we had an issue. The engine firstly wouldnt idle under 2500 rpm. Then it wouldnt start. The condensation was blown out with air. Then Daniel found a leak between the custom manifold and the base adapter plate. I recognised that spot. The gasket and hence the gasket goo area was less than 3mm wide between the intake neck and the mounting stud.
So we packed up our box of tricks and decided I'd remake the manifold. Daniel supplied me with some 75mm pipe and a leice of 75mm silicome tube.
Homewood bound and the difference was- well extraordinary particularly acceleration between 80-110 kph. Truly quick by previous standards. Tackling hills is a breeze where previously I'd drop speed to say 80kph or even drop down to second the trike maintains 100 kph effortlessly. When the trike does hit a slower steeper incline and drop down to second the front of the trike lifts. Not off the ground at that speed say 60kph but you do get that sensation of the machine sitting on its haunches- nice. Timing was eventually set at about 12 degrees which surprised us. And no pinging on the way home that I could detect. And the advance left alone.
Boost max indicated was 5psi. I think I'll be happy with that. I wont rule out at a later time changing the SC pulley to a slightly smaller one to get a bit more boost but I'll leave it alone for some time yet.
Now to rebuild that manifold and get the manifold between the Sc and the carbie shortened to make way for a wider air box
[SIGPIC][/SIGPIC]Tweety trike- EA81 (full reco 2014) 32/36 weber, SPFI manifold, 9.5:1 CR, VW auto.