Yeah D have replaced that too :P did notice it help a little. On a note decided to run with some 98 octane to see if it might help a little and while I am still only running 10 degrees and I didn't obviously get the power gains for it I did return a better economy of roughly 10L per 100 with mostly town driving, this was prior to fuel filter and engine cleaner being sprayed.
and now the list of replacements I have done in the past 3 months and despite this still have misfire (some are totally unrelated though I think):
Plugs (brand new)
Leads (brand new)
Rotor button (brand new)
Air filter (brand new)
fuel filter (brand new)
Timing belt kit (brand new)
Oil Pump seals (brand new)
fan belts (brand new)
trans axle seals (brand new)
Rocker cover Gaskets (brand new)
Water pump (brand new)
Sump Gasket (brand new)
Oil filter an oil (brand new 20/W50 gulf western oil.
spayed upper engine cleaner through it today which improved the idle but there is still an unpleasant miss fire there.
I am wondering maybe I have split a Vacuum hose? either that or my carby needs a rebuild car has only done 181 000kms? Or I have put mucked up a Vacuum hose and crossed them up?
Next items on my list (feels like it gets bigger

lol).
14 inch rims
Carby rebuild
Replacing vacuum hoses a meter at a time lol
Automatic transmission service
left and right ball joints
tires n wheel alignment.
coil
Dissy Cap
thermostat
Radiator + hoses
Aircon conversion R134A an gas
Tinted windows.
(All hopefully this year).
big out there post I know but just putting down what I've done and what I plan to do.